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30 Posts
Got the 06 mega 1 year ago and now it has 101,000 miles on it and a slight tapping sound. Put it in the shop for oil and filters change. Had the mechanics do a valve adjustment too. Now after the valve adjustment it has no power. RPMs would not go over 1200 at WOT. Got good boost, fuel, and pedal readings on the CTS. Truck ran fine before I took it in to the shop. At first they said there was to much play in the main shaft in the turbo and it was not building boost and that was the problem. Got a BD single. Problem still there. Now they say low compression "international engine problem". I think they botched the valve lashing and it's loosing the compression that way.
anyone with experience doing valve adjustments know if those symptoms could be caused by a botched adjustment?
anyone with experience doing valve adjustments know if those symptoms could be caused by a botched adjustment?